|
The following information is provided to assist any service personnel in the replacement of the main transformer. It is assumed that the personnel are familiar with all safety precautions and that they have prior experience with this or similar equipment. It is further assumed that the personnel understands basic electronics and they are familiar with the terms used in this procedure. |
Symptoms of a bad transformer are usually obvious. The
customer generally describes them as one or ALL of the following.
|
| It's not a good idea to plug in a welder with these symptoms!! I generally start by removing all the covers and visually inspect the entire welder from AC input to the welding power output. |
| In the case of the following welder, I do not believe that the customer was being totally honest with me when he brought it in. The unit was still under factory warranty and I think he thought it best not to divulge much information less he be blamed for the failure. He should have been aware of one or more of the above symptoms, but he mentioned none. In fact, he said he was just welding along and it quit. He said that it had done this before and he would wait awhile and it would start up again. That's usually a symptom of exceeding the duty cycle of the welder and too much of that can be a bad thing (i.e. transformer and/or the rectifier overheating) |
I
started here by removing the covers, and it became apparent right away
that the transformer was burned up. There were obvious burn marks on the
transformer insulation wrap that surrounds the winding.
In order to get to all the transformer mounting bolts, I loosened the front panel and pulled it away as far as I could. I unplugged the circuit board and also detached the rate control switch from the front panel. Next I labeled all the wires and disconnect the transformer from the rectifier. I left the rate control attached to the transformer and disconnected only the wires necessary to allow the rate control switch to come out with the transformer (see photo below.) |
The
photo on the right shows the the burned windings. As you can see, its the secondary
winding (outer winding connected to rectifier) that is damaged. Usually
when a transformer goes bad, it is the primary winding (inner
winding connected to rate control switch) that burns.
I have found that when the primary winding fails, I usually find a shorted rate control switch or that the customer connected the machine to the wrong input line voltage. There's not much protection that can save a transformer from those two situations. The secondary winding failure is a different story, however. Cooling fans and thermal overloads are generally sufficient to save the transformer from component failure (like a shorted rectifier diode) or from the user exceeding the duty cycle of the machine. Situations like this warrant further investigation (i.e. checking the fan motor, rectifier, overload, etc..) |
This
rectifier assy (shown left) is composed of six diodes. Four are in a bridge
configuration and two are connected
connected across the transformer secondary with their anodes in common.
The numbers show the relationship between the photo and diagram |
Since
the secondary winding was burned, I checked the rectifier assy for short
circuits. With all the leads disconnected from the rectifier (except the
negative output), I checked across each diode. With my VOM set on X1000
scale, I looked for a high resistance one way and then reversed the VOM
leads and looked for a low resistance the opposite direction. I found
no shorted diodes. The fan checked okay, also. |
When I checked the
thermal overload, I found (much to my surprise) that it was open.
Since the overload prevents the transformer from operating, the only thing
I could think of that would cause this situation would be if the overload
had been cycling on and off (due to the transformer being hot) and it
eventually broke down. Like I mentioned before, I still think the customer
new more than what he was letting on. |
The
new transformer came with a rate control switch already connected. This
makes changing the transformer much easier, and it eliminates the possible
damage to the transformer that would occur if it was connected improperly.
|
|
The new transformer, rate control switch, and thermal overload; put this welder back in operating condition. |